[1] 郭海滨,左秀荣,张新理,等.奥氏体化温度对奥氏体晶粒度及第二相固溶的影响[J].钢铁研究学报,2016,28(2):63-68. Guo Haibin,Zuo Xiurong,Zhang Xinli,et al.Effect of austenitizing temperature on size of austenite grain and solid solution of second phase particles [J].Journal of Iron and Steel Research,2016,28(2):63-68. [2] 樊 晨,刘中程,蔡开科,等.BOF-LF-CC工艺生产45号钢钢水结构洁净度的研究[J].钢铁,2003,38(3):18-20. Fan Chen,Liu Zhongcheng,Cai Kaike,et al.Research on cleanliness of steel grade 45 produced by BOF-LF-CC process[J].Iron and Steel,2003,38(3):18-20. [3] 钟 彬,陈义庆,孟凡磊,等.N80油管穿孔失效原因分析[J].腐蚀与防护,2018,39(8):647-650. Zhong Bin,Chen Yiqing,Meng Fanlei,et al.Perforation failure analysis of N80 pipe[J].Corrosion and Protection,2018,39(8):647-650. [4] 彭 成,黄福祥,梁 爽,等.固溶处理温度对高硅锰铬镍奥氏体不锈钢晶间腐蚀的影响[J].金属热处理,2019,44(6):128-132. Peng Cheng,Huang Fuxiang,Liang Shuang,et al.Effect of solution treatment temperature on intergranular corrosion of high silicon manganese chromium-nickel austinitic stainless steel[J].Heat Treatment of Metals,2019,44(6):128-132. [5] 张 毅,袁鹏斌,高连新.油井管失效分析[M].北京:石油工业出版社,2015:145-149. [6] 潘健生,周敬恩,王广生,等.热处理手册[M].4版.北京:机械工业出版社,2008:100-109. [7] 樊东黎,徐跃明,佟晓辉.热处理数据手册[M].北京:机械工业出版社,2006:318-322. [8] 姜如松,廖永红.40CrMnMo钢单体泵泵体淬火开裂分析及对策[J].金属热处理,2016,41(12):187-195. Jiang Rusong,Liao Yonghong.Quenching crack analysis and counter measures of 40CrMnMo steel single pump body[J].Heat Treatment of Metals,2016,41(12):187-195. [9] Sen S,Aksakal B,Oze A L.Transient and residual thermal stresses in quenched cylindrical bodies[J].International Journal of Mechanical Sciences,2000,42:2013-2019. [10] 谷 曼.热处理工艺中淬火裂纹的预防[J].合肥联合大学学报,2001,11(1):100-105. Gu Man.The prevention of quenching crackles in heat-treating technology[J].Journal of HeFei Union University,2001,11(1):100-105. |